Influence of ammonia on wet-limestone flue gas desulfurization process from coal-based power plant

The paper presents data concerning the influence of ammonia on wet flue gas desulfurization (WFGD) absorber. Paper presents preliminary results of an industrial scale study on WFGD absorber, that collects flue gases from four boilers with total flue gas flow capacity of the WFGD equal to 1 500 000 N...

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Bibliographic Details
Main Authors: Wypiór Tomasz, Krzyżyńska Renata
Format: Article
Language:English
Published: EDP Sciences 2019-01-01
Series:E3S Web of Conferences
Online Access:https://www.e3s-conferences.org/articles/e3sconf/pdf/2019/42/e3sconf_asee18_00101.pdf
Description
Summary:The paper presents data concerning the influence of ammonia on wet flue gas desulfurization (WFGD) absorber. Paper presents preliminary results of an industrial scale study on WFGD absorber, that collects flue gases from four boilers with total flue gas flow capacity of the WFGD equal to 1 500 000 Nm3/h. Each boiler is equipped with selective non-catalytic reduction (SNCR) with urea injection. It was shown, that ammonia present in the flue gas upstream the WFGD increases the pH of absorption slurry, impacting the desulphurization process. In addition, analysis of particulate matter upstream and downstream the absorber shows an increase of the concentration of ammonium species in the particulate matter about 14 times, as average. Moreover, a non-optimized denitrification process can cause a high NH4+ concentration in the absorption slurry (up to 768 mg/L) and raw wastewater (up to 891 mg/L).
ISSN:2267-1242