Air staging application effects on overall steam boiler operation

This paper presents the results of calculation system of main processes in power steam boiler, before and after application of air staging. Modified air injection scheme was implemented during 2015 on the power steam boiler within unit 1 of TPP Kostolac B. Measurements performed on site showed that...

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Main Authors: Stupar Goran M., Tucaković Dragan R., Živanović Titoslav V., Belošević Srđan V., Crnomarković Nenad Đ.
Format: Article
Language:English
Published: VINCA Institute of Nuclear Sciences 2019-01-01
Series:Thermal Science
Subjects:
nox
Online Access:http://www.doiserbia.nb.rs/img/doi/0354-9836/2019/0354-98361900286S.pdf
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spelling doaj-2a395cf228eb4dc79895da6214d2be6f2021-01-02T12:04:32ZengVINCA Institute of Nuclear SciencesThermal Science0354-98362019-01-0123Suppl. 51559157410.2298/TSCI180413286S0354-98361900286SAir staging application effects on overall steam boiler operationStupar Goran M.0Tucaković Dragan R.1Živanović Titoslav V.2Belošević Srđan V.3Crnomarković Nenad Đ.4Faculty of Mechanical Engineering, University of Belgrade, Belgrade, SerbiaFaculty of Mechanical Engineering, University of Belgrade, Belgrade, SerbiaFaculty of Mechanical Engineering, University of Belgrade, Belgrade, SerbiaVinča Institute of Nuclear Sciences, University of Belgrade, Belgrade, SerbiaVinča Institute of Nuclear Sciences, University of Belgrade, Belgrade, SerbiaThis paper presents the results of calculation system of main processes in power steam boiler, before and after application of air staging. Modified air injection scheme was implemented during 2015 on the power steam boiler within unit 1 of TPP Kostolac B. Measurements performed on site showed that applied reconstruction led to a permanent loss of the steam boiler power. This study was performed in order to define the cause of such an occurrence and to consider the possibility for regaining the designed steam parameters along with keeping NO concentration in prescribed limits. This paper x discusses the influence of repositioning the air injection location on processes within the furnace. Furthermore, the influence of the redistribution of injected air-flow along the furnace height on important boiler operation parameters has been analyzed. Analysis showed that, with appropriate dosing of air along the height of the existing furnace, it is possible to achieve the optimum of the boiler's operation parameters. Results of research showed that air staging throughout the furnace height in best test case additionally reduces NO concentration (195-225 mg/Nm3) and increases the power of x considered boiler (828.8-751.1 MW) with an insignificant decrease of the boiler's efficiency (86.27-86.77%). Furthermore, the designed temperatures of superheated (540-498°C) and reheated (540-518°C) steam have been reached again, whereby the safety of the boiler's operation has been significantly increased. Results of this study improve the present explanation of the processes occurred in the furnace with applied primary measures. They also give directions on defining the most influential parameters on considered processes with the final purpose to increase the efficiency and availability of the entire plant. [Project of the Serbian Ministry of Education, Science and Technological Development, Grant no. TR-33018: Increase in energy and ecology efficiency of processes in pulverized coal-fired furnace and optimization of utility steam boiler air preheater by using in-house developed software tools]http://www.doiserbia.nb.rs/img/doi/0354-9836/2019/0354-98361900286S.pdfair stagingpower steam boilernoxsub-stoichiometric
collection DOAJ
language English
format Article
sources DOAJ
author Stupar Goran M.
Tucaković Dragan R.
Živanović Titoslav V.
Belošević Srđan V.
Crnomarković Nenad Đ.
spellingShingle Stupar Goran M.
Tucaković Dragan R.
Živanović Titoslav V.
Belošević Srđan V.
Crnomarković Nenad Đ.
Air staging application effects on overall steam boiler operation
Thermal Science
air staging
power steam boiler
nox
sub-stoichiometric
author_facet Stupar Goran M.
Tucaković Dragan R.
Živanović Titoslav V.
Belošević Srđan V.
Crnomarković Nenad Đ.
author_sort Stupar Goran M.
title Air staging application effects on overall steam boiler operation
title_short Air staging application effects on overall steam boiler operation
title_full Air staging application effects on overall steam boiler operation
title_fullStr Air staging application effects on overall steam boiler operation
title_full_unstemmed Air staging application effects on overall steam boiler operation
title_sort air staging application effects on overall steam boiler operation
publisher VINCA Institute of Nuclear Sciences
series Thermal Science
issn 0354-9836
publishDate 2019-01-01
description This paper presents the results of calculation system of main processes in power steam boiler, before and after application of air staging. Modified air injection scheme was implemented during 2015 on the power steam boiler within unit 1 of TPP Kostolac B. Measurements performed on site showed that applied reconstruction led to a permanent loss of the steam boiler power. This study was performed in order to define the cause of such an occurrence and to consider the possibility for regaining the designed steam parameters along with keeping NO concentration in prescribed limits. This paper x discusses the influence of repositioning the air injection location on processes within the furnace. Furthermore, the influence of the redistribution of injected air-flow along the furnace height on important boiler operation parameters has been analyzed. Analysis showed that, with appropriate dosing of air along the height of the existing furnace, it is possible to achieve the optimum of the boiler's operation parameters. Results of research showed that air staging throughout the furnace height in best test case additionally reduces NO concentration (195-225 mg/Nm3) and increases the power of x considered boiler (828.8-751.1 MW) with an insignificant decrease of the boiler's efficiency (86.27-86.77%). Furthermore, the designed temperatures of superheated (540-498°C) and reheated (540-518°C) steam have been reached again, whereby the safety of the boiler's operation has been significantly increased. Results of this study improve the present explanation of the processes occurred in the furnace with applied primary measures. They also give directions on defining the most influential parameters on considered processes with the final purpose to increase the efficiency and availability of the entire plant. [Project of the Serbian Ministry of Education, Science and Technological Development, Grant no. TR-33018: Increase in energy and ecology efficiency of processes in pulverized coal-fired furnace and optimization of utility steam boiler air preheater by using in-house developed software tools]
topic air staging
power steam boiler
nox
sub-stoichiometric
url http://www.doiserbia.nb.rs/img/doi/0354-9836/2019/0354-98361900286S.pdf
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AT zivanovictitoslavv airstagingapplicationeffectsonoverallsteamboileroperation
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