Optimization of carbonate reservoir well testing
The purpose of the paper is to design a workflow for well testing to optimize the time of study and reduce the switch-off period of wells in a pilot test. Another puprose is to confirm the economic efficiency of the presented workflow. Wells T-23, T-361, T-388 of the A-field were used as objects of...
Main Authors: | Аnastasiya E. Davydova, Aleksandr A. Shchurenko, Nikita M. Dadakin, Artyom D. Shutalev, Bronislav B. Kvesco |
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Format: | Article |
Language: | English |
Published: |
Perm National Research Polytechnic University
2018-06-01
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Series: | Perm Journal of Petroleum and Mining Engineering |
Subjects: | |
Online Access: | http://vestnik.pstu.ru/get/_res/fs/file2.pdf/7493/Optimization+of+carbonate+reservoir+well+testingfile2.pdf |
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