Empirical Study of Foundry Efficiency Improvement Based on Data-Driven Techniques

In this paper, a data-driven approach was applied to improve a furnace zone of a foundry in Taiwan. Improvements are based on the historical production records, order-scheduling, and labor-scheduling data. To resolve the bottleneck provided by the company, historical data were analyzed, and the exis...

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Main Authors: Kuentai Chen, Chien-Chih Wang, Chi-Hung Kuo
Format: Article
Language:English
Published: MDPI AG 2021-06-01
Series:Processes
Subjects:
Online Access:https://www.mdpi.com/2227-9717/9/7/1083
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spelling doaj-eae666e031544a9f86df1c2a241338442021-07-23T14:02:53ZengMDPI AGProcesses2227-97172021-06-0191083108310.3390/pr9071083Empirical Study of Foundry Efficiency Improvement Based on Data-Driven TechniquesKuentai Chen0Chien-Chih Wang1Chi-Hung Kuo2Department of Industrial Engineering and Management, Ming Chi University of Technology, New Taipei City 243303, TaiwanDepartment of Industrial Engineering and Management, Ming Chi University of Technology, New Taipei City 243303, TaiwanDepartment of Industrial Engineering and Management, Ming Chi University of Technology, New Taipei City 243303, TaiwanIn this paper, a data-driven approach was applied to improve a furnace zone of a foundry in Taiwan. Improvements are based on the historical production records, order-scheduling, and labor-scheduling data. To resolve the bottleneck provided by the company, historical data were analyzed, and the existence of large variance in the process was found. Statistical analysis was performed to identify the primal factors causing the variance, and suggestions were made and implemented to the production line. As a result, daily production increased steadily to more than 30 pots of molten metal, while the original production was 20–30 pots of molten metal and are not controllable. Such significant improvement was mainly made by standardizing the input and reducing the variance of processes. The average cycle time of each pot of molten metal was reduced from 219 min to 135 min. Our suggested improvements also reduced the foundry’s electricity consumption cost by almost $240,000NT per month. In summary, data analysis can help traditional industries in identifying the main factors causing the bottleneck.https://www.mdpi.com/2227-9717/9/7/1083bottlenect detectionstatistical data analysisprocess variationproductivitycasting
collection DOAJ
language English
format Article
sources DOAJ
author Kuentai Chen
Chien-Chih Wang
Chi-Hung Kuo
spellingShingle Kuentai Chen
Chien-Chih Wang
Chi-Hung Kuo
Empirical Study of Foundry Efficiency Improvement Based on Data-Driven Techniques
Processes
bottlenect detection
statistical data analysis
process variation
productivity
casting
author_facet Kuentai Chen
Chien-Chih Wang
Chi-Hung Kuo
author_sort Kuentai Chen
title Empirical Study of Foundry Efficiency Improvement Based on Data-Driven Techniques
title_short Empirical Study of Foundry Efficiency Improvement Based on Data-Driven Techniques
title_full Empirical Study of Foundry Efficiency Improvement Based on Data-Driven Techniques
title_fullStr Empirical Study of Foundry Efficiency Improvement Based on Data-Driven Techniques
title_full_unstemmed Empirical Study of Foundry Efficiency Improvement Based on Data-Driven Techniques
title_sort empirical study of foundry efficiency improvement based on data-driven techniques
publisher MDPI AG
series Processes
issn 2227-9717
publishDate 2021-06-01
description In this paper, a data-driven approach was applied to improve a furnace zone of a foundry in Taiwan. Improvements are based on the historical production records, order-scheduling, and labor-scheduling data. To resolve the bottleneck provided by the company, historical data were analyzed, and the existence of large variance in the process was found. Statistical analysis was performed to identify the primal factors causing the variance, and suggestions were made and implemented to the production line. As a result, daily production increased steadily to more than 30 pots of molten metal, while the original production was 20–30 pots of molten metal and are not controllable. Such significant improvement was mainly made by standardizing the input and reducing the variance of processes. The average cycle time of each pot of molten metal was reduced from 219 min to 135 min. Our suggested improvements also reduced the foundry’s electricity consumption cost by almost $240,000NT per month. In summary, data analysis can help traditional industries in identifying the main factors causing the bottleneck.
topic bottlenect detection
statistical data analysis
process variation
productivity
casting
url https://www.mdpi.com/2227-9717/9/7/1083
work_keys_str_mv AT kuentaichen empiricalstudyoffoundryefficiencyimprovementbasedondatadriventechniques
AT chienchihwang empiricalstudyoffoundryefficiencyimprovementbasedondatadriventechniques
AT chihungkuo empiricalstudyoffoundryefficiencyimprovementbasedondatadriventechniques
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