Behavior and Simulation of Pumping Induced Drawdown in the MRT Taipei Bridge Station

碩士 === 國立臺灣科技大學 === 營建工程系 === 95 === The main objective of this study is to investigate the suitability of linear superposition and numerical method in the simulation of pumping induced drawdown. In the past, there were few large scale cases about deep excavation with pumping groundwater and therefo...

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Bibliographic Details
Main Authors: Zeng-Wei Gong, 曾為恭
Other Authors: Chang-Yu Ou
Format: Others
Language:zh-TW
Published: 2007
Online Access:http://ndltd.ncl.edu.tw/handle/vmh5yx
Description
Summary:碩士 === 國立臺灣科技大學 === 營建工程系 === 95 === The main objective of this study is to investigate the suitability of linear superposition and numerical method in the simulation of pumping induced drawdown. In the past, there were few large scale cases about deep excavation with pumping groundwater and therefore the case study of using linear superposition and numerical simulation of drawdown in pumping groundwater by group wells is not too much. In this research we use the cases of the pumping induced drawdown in the MRT Taipei Bridge Station. According to the results of single well test, the hydraulic parameters of Chingmei Formation in Taipei are obtained. Then the linear superposition method is used to simulate the drawdown by group wells test and actual excavation pumping. The result of simulation by linear superposition was close to field data. In numerical simulation, we adopt the computer program PMWIN to simulate the pumping induced drawdown, with the consideration of the 2D horizontal single layer. Results show that drawdown from PMWIN is close to those from superposition and field measurements.